視覺跟蹤在數(shù)控加工智能產(chǎn)線中的應(yīng)用研究

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中圖分類號(hào):TP242.2 文獻(xiàn)標(biāo)志碼:A 文章編號(hào):1671-5276(2025)03-0121-05
Research on Application of Visual Tracking in Intelligent Production Line of CNC Machining
HU Weifeng,HAN Wei,YAN Jian,LIU Jianguang
(School of Mechanical Engineering,Guangzhou City Universityof Technology,Guangzhou 5108Oo,China)
Abstract:Concerning theknow-howof robotsaccurately grasping partsrandomlyand disorderlyplacedontheconveyor belt duringtheoperationofflexibleCNCmachining production lines forautomotiveengines,thevisual control position trackigof FANUC visionsystemandthetechnical methodsofrobotrapid positioningand grasping of parts were studied.The proces of generatingvisual inspectionimagedataforparts placedindisorderontheconveyorbeltthroughmultiplecamerasandthe method of zeropointcalibrationand imagingparameterseting forthevisual systemcamera wereanalyzed.TheFANUCmacroprogram wasused tofittheimagingdataof twocamerasandgenerateapartpositioncordinatesystem,andthepositionoffsetdataof randomlyplacedpartswasdeterminedbycomparingandcalculating thestandard positioning template,so thattherobot coordinate system tracking,gripperposition adjustment,and part grasping program were developed,which improves the accuracy and reliability of CNC machining production line positioning.
Keywords:inteligent production line;robot;vision calibration;coordinate tracking;ofset compensation
0 引言
為了提高汽車制造企業(yè)的生產(chǎn)效率和智能化水平,在大批量的汽車發(fā)動(dòng)機(jī)缸蓋、缸體和減速箱蓋等鋁合金零件的柔性數(shù)控加工過程中,正在推廣使用機(jī)器人自動(dòng)上下料的方法,將傳送帶上的零件抓取送入或取出機(jī)床工作臺(tái)。(剩余5014字)